

Electric Power on the Shearwater II,
Updates in July 2001and January 2004
Everyone who cruises in the summer in warmer climates
struggles with the management of electric power unless you make the decision to
“primitive camp” on the water. Our
home has a water maker, air conditioning, a refrigerator and separate freezer, a
microwave, and a washer/dryer combination.
If forced to choose what we would give up to save power, many of these would be
kept before our navigation lights and VHF when all the votes were counted.
Our power is generated, stored and delivered by a
DC/Inverter system assembled from common components. This section describes our experience with parts of that
system after about eight months of heavy use.
First, the important stuff:
Batteries
Voyage
delivered the Shearwater II
with 8 6-volt
225 Amp hour absorbed glass batteries (AGM) connected in a series/parallel
arrangement.
These replaced our original gel cell
batteries that were intended to be maintenance free but they used nearly two gallons of
distilled water since commissioning them in 2000.
In May, 2003, one of the serious
potential failures with large battery banks occurred. One cell of one
original 6-volt gel cell batteries internally shorted - reducing that battery's voltage to about 4
volts. The remaining three sets of 12-volt batteries (formed by placing
two 6-volt batteries in series) tried to charged the failed cell. The
resultant heat, boiling acid, and smoked charred both battery boxes, filled one
cabin with acidic gas and could have been very serious had it continued.
Fortunately, we turned the master "A"-"B"
switch OFF, disconnected the offending battery and assessed the damage.
400 Ah of our total 800 Ah was damaged beyond salvation. We were in Havana
at the time.
We sailed to Galveston and replaced the
800 Ah of Gel Cells with 900 Ah of AGM batteries. The new AGMs used the same space
as the old Gel Cells but, unfortunately, were not delivered with the terminals
we ordered. We had
requested
bolt-thru "L" type terminals and were delivered batteries with holes tapped for
1/4-20 bolts. Short copper bolts were also delivered making it quite hard
to bolt on the wires required by our installation. Because of the lead
length in a catamaran - up to 40' round trip - and the limited sizes of the wire
chases, two red and two black wires were run from each bank of two sets of
6-volt batteries to the master "a"-"b" switch. An additional set of red
and black "00" batteries (lower right) were run to the engine closest to that
portion of the bank - a run of about 12 feet round trip. Finally, the two
sets of 6-volt batteries were joined into a 12-volt battery with a 1/4" by 1"
strip of copper bus bar. We used this rather than wire to limit the height
of the stack so the battery box door would close. and required
significant re-work before placing them in full service.
Alternators
Voyage delivered the
Shearwater II with two 55 Amp
alternators, one on each engine. We use these primarily for charging the
dedicated starting batteries, again one for each engine.
We have added a Balmar 95-210 210 Amp alternator
to each Yanmar 3GM (27 HP) engine. These
alternators each were intended to generate sufficient current to operate an air conditioner (via
an inverter) and slightly charge the house battery bank.
The
only significant change to the original charging circuit is the installation of a wire from the engine control
circuit to supply power (exciter power) the regulator of the new alternator.
This circuit demands a maximum of about 8 amps for all regulator functions -
thus is unlikely to significantly effect the charging operation of the engine
battery.
Field current, a maximum of about six Amps, is drawn from the
engine start battery to a new regulator and then to the new
alternator. A Balmar 95-210 Amp large
frame Alternator is attached. A
heavy-duty double belt drive system is used to transfer about 8hp (maximum) from
the engine. We find that Carquest Green Striped grove belts last about 1000
hours in normal operation and require adjusting about every 50 hours or so.
Power to the new regulator is supplied by the "key"
on each engine. When starting the engine cold, I normally crack
the throttle a hair, engage the starter, and turn the key off after the engine
starts so the engine can
warm up with no load. Once the engine has warmed sufficiently (about 2
minutes), I turn on the key and activate both the factory original and new
alternators - the original alternator recharges the starting battery and
supplies a small amount of current to the new regulator while new alternator supplies power to the house bus and the house battery.
We use two Balmar 612 alternator
controllers (voltage regulators), one on each engine. These regulators
permit a setting of initial delay to permit warm-up of the engine before engaging
the new alternator. This delay starts after the key is turned on - so in
our case, the original alternator is engaged and 45 (adjustable) seconds later
the new, larger, alternator load is applied to the engine.
Each new alternator is connected to 1/2 the battery
bank (about 450 Ah) by a set of "00" marine grade cables. The
cables are fused at 250 Amps, and there are no switches in the charging link.
There is about 12 feet of cable in the round trip between the house alternator
and the half of the house bank charged by that alternator.
Voyage also augmented the boat's wiring by placing a second
set of heavy (about 1 gauge) wire in parallel with the battery wire
originally supplied after we determined the original battery wire was undersized
for our load.. Out total system voltage drop at worst case (low
batteries, one alternator running, and a heavy load such as the washer/dryer) is
only about 0.2 volts. There is no detectable heating on any connection
except the radiated heat from the alternator.
Should full engine power be needed in an “emergency”,
simply shut off the engine switch withdrawing power to the alternator field.
Actually, both the 55 amp and the new house alternator are shut off, but the
original
55 amp alternator
normally places only an insignificant load on the engine because the starting
battery is usually fully charged and there is minimal equipment on the starting
circuit.
During simulated emergency practice with
100 hours on each engine, there was a clearly observed
reduction in the engine load but no corresponding increase in boat speed.
I suspect the engine is incapable of being throttled to absolutely full
output in our installation and the removal of the alternator load is adjusted
automatically by a reduction in the governor’s feed of fuel to the engine.
I’m not sure of this – only that full cruising power, RPM and speed seem to be available
even when the alternator is supplying significant power to the battery bank and
inverter.
As the engines have aged (about 4000
hours since 2000), the alternators now cause a slight reduction in RPM at cruising
speed - from about 3200 RPM to about 3150 RPM when the key is turned on and the
45 second regulator timer expires. This aging turned out to be the first
symptoms of engine failure.
Unfortunately, the Balmar alternators
have proven to be unreliable in our environment of heavy use at nearly full
power. While they would probably be quite satisfactory for charging
batteries, we demand nearly full power over an extended period when operating
our washer/dryer or air conditioning. The heat and load ages them quickly.
Between 2000 and 2004, we have had 3
rebuilds on each alternator. Each rebuild cost us between $250 and $550
per rebuild - more than the original cost of the alternator over only a three
year life.
See the Zena page
for our current charging solution.
Inverter
The next critical part of our system is a 3000-Watt Prosine
inverter. This is a combination
battery charger, inverter, and power switching system.
It automatically detects the delivery of shore power from the dock and
synchronizes the inverter-generated power before cutting over to shore power.
Thus, our computer and air conditioner usually continue to operate without
interruption when plugging in after a sail.
This is a no-switch system. Arrive
at the dock, plug in the shore power cord, have a beer.
Time to go? Unplug the shore
power cord and sail away.
The air conditioner operates between four and six hours on
battery depending on how many minutes of each hour the compressor operates
to provide the necessary cooling. The
computer operates about three days on battery power if the engine is not
operating and the air conditioning is not on.
One engine at 2500 rpm or more is sufficient to operate the air
conditioner indefinitely and maintain a DC bus voltage of about 12.5 Volts.
This “costs” about one liter per hour, maybe one-half a buck at
today’s rates. Not bad for air
conditioning in the middle of nowhere by an engine that is so quiet we can
hardly hear it above the normal boat noises with the air conditioning running.
Boats sharing our anchorage can hardly hear it from a boat length away.
A few minutes operation of the microwave requires no engine
support.
The washer/dryer requires engine operation when in use away
from shore power. I normally start
a second engine at about 1500 rpm if the washer/dryer and air conditioning are
both in use. One engine at about
2500 rpm will carry both loads and maintain about 12.3 Volts on the bus – with
the computer running. This is our
normal mode when under way. Yep –
we run one engine, maintain just over five knots, and can support both the
washer/dryer and air conditioning – all for about one-half gallon per hour.
The house batteries are not charged in this environment - all the output goes to
the inverter.
Two engines at 2500 rpm each get us just over six knots, raises the bus
voltage to about 13.8 and will operate everything on board while supplying full
power to the props, and charge the house bank. We always
maneuver on two engines.
John Zeitlin,
http://www.zrd.com/,
supplied the Balmar alternators, regulators, and installation kit that went to
South Africa with us when we commissioned the new Shearwater II.
He is also continuing to research our two minor problems that remain.